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An Old Marlin Brought Back To Life

By: Steve Ostrem

Got a great old gun that you’d love to shoot if only the rifling was in better shape? I have an 1889 Marlin lever gun in .38-40 that has seen better days, to put it mildly. The bluing has turned to rust and some of the parts are missing, or need to be replaced. The worst part however, is the rifling, or what remains of it. The inside of the barrel looks like a piece of sewer pipe in which the pits form a spiral. To grade it at NRA "Poor" would be charitable to say the least. The trouble is, it’s a really neat gun, (Marlin’s first side-eject design), and I’d like to be able to shoot it and occasionally hit the target.

After years of letting this fine old piece of history sit idly in the corner, I decided to re-line the barrel and make it shoot again. Luckily for me, this job has never been easier with the selection of special liners and drills for this purpose that we have today. We also have a Barrel Liner Instruction Book (#077-200-143) which is available at no charge and explains re-lining .22 barrels along with a short section on installing a centerfire liner. It describes using Force 44 solder or Acraglas® (#081-003-002) to secure the liner in place and has a lot of good information from three different gunsmiths who share their time-proven methods.

The first thing I did was round up a 38-40 liner and the proper piloted drill. There are two drills available for the liners we carry, a long drill and a shorter version for those who want to add their own extension. I chose the long drill, as it was just long enough to do my 24-inch barrel without adding an extension. (13 inches-not including the pilot). The liner measured about 25 inches long, which is just about right. It’s good to have a little excess to cut off at each end to be sure the rifling is clean and undamaged. Once you have the proper chambering reamer, you are almost set to go. There is still the matter of how to secure the liner in the barrel. Soldering is the traditional method, but using Acraglas is much easier and does not pose any danger to the existing finish on the gun as heating it with a torch might. Another advantage to Acraglas is that when mixed with black dye it becomes extremely hard to see the seam between the barrel and the liner. My barrel needed to be refinished anyway, so I thought I’d make this project really interesting and use the solder-in method.
Drilling the barrel can be done in the lathe or with an electric hand drill, and a good job can be done with either method. Don’t bother with smaller _” and 3/8”drills. They simply do not have the power to do this job. Also, remember to use a good cutting fluid such as Universal Do-Drill™ (#083-007-016). This helps the drill cut smoother and much easier with less tendency to clog or hang up in the hole. It also helps the drill bit cut a nice round hole to the proper size resulting in a good liner-to-barrel fit.


On this particular barrel, the breech has an overhanging hood that makes drilling difficult. Therefore, I decided it would be better to put it in a lathe and use a boring bar to start the hole at the breech. I found a piece of brass rod and turned it down until it just fit what remained of the rifling. This allowed me to run an indicator on the rod, and true up the barrel in the four-jaw chuck, thereby insuring the hole I was turning with the boring bar would be concentric with the rifling. It is also possible to make a bushing to fit the old chamber to support the pilot portion of the drill until there is metal all the way around to keep the drill on course at the beginning. In this case, however, it was simply quicker to open up the breech end for about the first half-inch with a boring bar to the major diameter of the drill, (.590”), and then continue on with the drill. This prevents the drill from making an over-size or egg-shaped hole, which would surely happen anywhere the tool is not cutting metal all the way around.

The muzzle presented no such problem, of course, but while drilling the front of the barrel the drill did break through the bottoms of the two dovetails for the front sight and the magazine tube stud. This doesn’t hurt anything and will be invisible once the gun is put back together. Just be careful when withdrawing the drill with the machine running as sometimes a chip will catch in this opening and try to pull the drill back in. Once the chips started building up in the barrel, it worked better to retract the drill about an inch under power and then turn the machine off to remove it completely. With the barrel turning at 90 rpm the drill cut very smoothly and evenly as long as I cleared the chips frequently and applied liberal amounts cutting oil. Then it was just a matter of going until the whole drill disappeared into the barrel, swapping ends, and doing it all over again from the other side until the holes met. Once you’re through, clean out the chips with a brush or swab on a cleaning rod and try sliding the liner in place. If it doesn’t go all the way into the barrel fairly easily you need to run the drill in again to remove any burrs or tight spots that may remain. Now is also a good time to sand the exterior surface of the liner to help it slide into the barrel and to provide a clean surface for the solder. When you are sure that the liner will slide into place without any problems it’s time to solder it in place.

I decided to tin the inside of the barrel first so that it could be laid aside while doing the liner without anything coming into contact with the soldered surface. With one end of the barrel clamped horizontally in the vise, the first step was to thoroughly clean the inside with a brush wrapped with patches soaked in TCE (#083-060-032) Once that was done, a brush wrapped in steel wool was soaked with Comet Flux #4 (#478-100-004), and run through the barrel to completely coat the interior. Then it was time to put the heat to it.

Using a standard propane torch, I began to heat the first six inches or so of the barrel until the Force-44™ Solder (#080-649-250) would flow when touched to the inside. I then fed more solder in until there was a pool of it in the resting in the bottom of the barrel. Using the cleaning rod with the steel wool-wrapped brush from the fluxing operation, I began to work the solder farther into the barrel and completely around the inside by moving the brush back and forth and rotating it at the same time. From time to time the brush froze in place where the metal was not quite hot enough, but it came free easily enough by applying a little more heat to that area. By slowly moving the heat father and farther along the barrel and adding more solder as needed I soon had the bore tinned past the halfway point. Then the tinned end was put in the vise and the operation was repeated on the other end until the entire length was coated. The barrel was then set aside to make room for the liner.

To tin the liner, I found a piece of brass rod and turned it down until it was a slip fit in the bore. I clamped the rod vertically in the vise and put the liner over it so it was standing straight up and could be rotated easily. I then gave it a good rubdown with a piece of steel wool saturated with Comet Flux. Starting at the top, the liner was heated with the torch until the solder would flow when touched to the surface. Remember, you want the hot metal to melt the solder, not the flame. Otherwise the solder will just ball up and fall off the part. Once there was a good bit of solder on the liner, I took the piece of steel wool with the flux in it and spread the solder around until it formed a thin, smooth coating on the metal. The solder went on quite easily as long as the metal was up to temperature. I did manage to stick my steel wool pad to the liner a couple of times, but with a little help from the torch it came free and I was able to continue on my way. I like to wear a new set of clean, white gloves for this operation so that I can turn the liner on its mandrel to get at the whole surface easily without getting burned and without contaminating my nice, freshly tinned part. I hardily recommend wearing gloves as well as eye protection when soldering and just the eye protection when drilling or operating a lathe. I used to be pretty indifferent about such precautions but after working in a couple of machine shops over the years I’ve seen some accidents that turned me into a firm believer. Anyway, the rest of the liner tinned beautifully and was now ready to be mated to the barrel.

Just to be different I took an old vise that I have mounted to a piece of board and put it on the floor with some weight on the board to secure it. I then put the mandrel used earlier for tinning the liner in the jaws so that I could stand the liner up on end as before. With this method you will need to plug the bore at the top to keep solder out. (I used a wad of tinfoil.) With the liner in place I lit the torch, positioned the barrel over the liner, and applied heat to both until the barrel started to slip over the liner. I figured that I’d make gravity work for me for once, and it seemed to work. By working the torch up and down portions of the barrel and liner and gradually increasing the amount of area brought up to temperature the barrel slowly began to move down onto the liner. With the liner resting on the mandrel, I was able to rotate it to distribute the heat evenly, (remember the gloves!) and make good progress. A rawhide mallet proved very useful to give the barrel a good rap from time to time to help things along. When there was only about a 1/2” of the liner left below the barrel it was time to stop.

This is the time to inspect the joint at the top and add solder if there are any gaps, and then turn the barrel around and do the same to the other end. Once I was satisfied with the solder job I put the hot barrel up in the bench vise and ran a brush and patches through it to remove any flux that may have wandered into the rifling. I had just gotten rid of one rusty bore and didn’t want another! Then I sat down to rest and to allow the newly assembled barrel and myself to cool off.

After things settled down a bit and the parts had cooled it was back to the lathe to turn the liner back until it was flush on both ends and recrown the barrel. Then came the fun part of trimming the breech section with files until the liner was even with the original metal. As you can tell from the picture, this took a little time. Then the barrel was chambered and headspaced in the usual manner and it was time to go to the range with my “new” rifle!

The first trip to the range, I must confess, was quite a disappointment. It was at the end of the day and the sun was low in the west, but still very bright. The brass bead on the new front sight I’d installed was fuzzier than usual, (old eyes), and the gun was printing all over the paper. I went home wondering if I’d somehow screwed up the liner or if it was the open sights giving me problems or both. That night I checked the barrel carefully for any clues. The bore was still bright and shiny and everything was as it should have been. All I could do was try again.

Luckily, the next day the sky was overcast and the wind was calm. I grabbed the gun and my dwindling supply of ammo and headed back to the range. This time it was a different story. I could actually see the front and rear sights and keep them aligned on the bullseye as I pressed the trigger. The first two shots were low and to the right so I adjusted the sights accordingly and the next three formed a nice tight group just to the right of the center dot. This was more like it! One more little correction for windage and then it was time for some serious plinking. Any dirt clod within 100 yards was in serious trouble at this point, with very few getting away as long as I remembered to allow for the 38-40’s parabolic trajectory. This is a very pleasant round to shoot with the low noise and recoil that it generates, and I happily blazed away until the ammo ran out and left me with no choice but to reluctantly pack everything up and head home with my “new” rifle. Of course, now that the gun is beautiful on the inside, the outside is going to need a complete makeover. I’ll let you know how that turns out.

Early on I had considered simply rebarreling the old Marlin with a brand new tube made of modern steel. This would mean losing the original markings on the barrel, which I really did not want to do. It would also mean turning a blank into an octagonal shape, cutting square threads for the breach, and cutting three dovetails in the barrel. That’s a lot of work! Besides, re-lining the barrel is the only way to restore accuracy and still preserve the gun to it’s original form, particularly for many of the older designs for which there are no original replacement barrels available. This holds true in the case of the rimfires as well. Brownells currently offers liners and drills for the .22 and .17 rimfires, and for the .25-20, .32-20, .38-40, and .44-40 in the centerfires, along with the necessary reamers and headspace gauges to go with them. Those fine old guns with bad bores no longer have to be regulated to “wall hanger” status, and can be made to shoot again and give many more years of service for successive generations.



List of materials used for this project:
Stock Numbers
Description
Redmond Barrel Liner (38-40)
Brownells .690" Barrel Liner Drill (38-40)
Manson Chamber Reamer (38-40)
1/4 lb. Force-44 Solder
No. 4 Comet Flux
Brownells TCE Degreaser
#00 Mild Steel Wool
.50 Caliber Brushes (3-Pack)
Clymer .38-40 Headspace Gauge (GO)
Clymer .38-40 Headspace Gauge (NO GO)
Gloves and eye protection.